Thrift Store Finds, Plastic Fixes, and What’s Next
Quick kettle update as we continue to tune, test, and improve:
Latest shipment:
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We shipped out 15 units recently.
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3 were exchanged by customers — we’re covering those quickly.
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Each kettle was tested three times during assembly, and 8 of 15 were re-tested stateside before shipment.
Plastic part breakthrough:
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We discovered the factory had changed the plastic used in the shuttle valve.
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We sourced our own high-quality plastic and re-shot the mold.
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Early signs show this is delivering higher yield and better reliability.
Vintage inspiration:
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A customer found a 1987 kettle at a thrift store in Michigan.
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I took it apart — it had melted through, but I’m comparing its internal parts against our current versions (weight, dimensions, feel, and finish) to guide improvements.
Next production run:
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We’re kicking off a batch of 100 more kettles (about 400 lbs of steel) for U.S. delivery.
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These will incorporate our latest part updates and process changes.
Post-purchase experience:
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A few customers mentioned the QR code for the troubleshooting video expired (it was tied to a paid service).
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The updated troubleshooting video is now freely available here: Watch the video
Looking ahead:
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I’ve started engaging UC Berkeley and Stanford to recruit Mandarin-speaking engineers for a stack-tolerancing analysis.
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Goal: make the kettle even more reliable — and tune the whistle for a richer, more robust sound.
Thanks again for following the journey — and for your continued support as we scale thoughtfully.
– Christian